...or the fitting at the rear of the manifold for vacuum lines was left off. Ken Quoting wrambler242@xxxxxxxxxxx: > Sounds like someone pulled the EGR tube and left the hole open? > Those run a flex tube from the exhaust to intake. They are often pulled > and plugged. Or robbed for running cars as they tend to twist into pretzel if > not taken off very carefully. > > Don't try to drive it anywhere at all till you get the drive shaft on. > There is a viscous coupling in that t-case and it will come undone. Not sure > they can be bought new anymore and they would be pricey to replace. > > > Sent from my BlackBerry® wireless device from U.S. Cellular > > -----Original Message----- > From: d stohler <das24rules@xxxxxxxxx> > Sender: amc-list-bounces@xxxxxxxxxxxx > Date: Thu, 30 Sep 2010 00:26:04 > To: <amc-list@xxxxxxxxxxxx> > Reply-To: "AMC, Rambler, Nash, Jeep and family" <amc-list@xxxxxxxxxxxx> > Subject: [AMC-list] IT RUNS!! (and idles pretty dang well now) > > ok, so my issues are getting solved on the new sx4. i was tinkerin with it > some more tonight. did what jim blair had said and swapped 1/6 plug wires to > make it backfire to blow out the carb. still didnt work after i put them > back. it backfired after that (it would do once in a while anyway) and i just > so happend to be looking at the carb when it backfired. and POOF!!! i saw a > bark of flame out the back side of the manifold next to the manifold/brake > booster. waddya know. there was a threaded hole where a plug or SOMETHING was > at one time. stuck a bolt in it to plug it for now. fired right up and idled > pretty dang nice. the stepper motor and micro switch on the choke are not > hooked up. so, i decided it was time to put the radiator in, and fill with > water. (didnt run it for more than 1-2 min dry and let it sit for about 1hour > after) filled it with water and let it idle for 1 hour or so. temp gauge wont > work. where is the sensor at? i cant find it. i had a > mechanical gauge dropped in the radiator cap hole. read solid 170* steady > once the t-stat opend. hooked up vacume line to the 4x4 stuff. clutch master > is gone, and rear drive shaft is out. try to slide into first, car wanted to > creap forward. so, feels like 4x4 might work. got the car for $125, have $35 > in parts in it now. i think im goin to have a CHEAP winter driver. need to > get all fluids changed before i drive it more than a mile from the house. im > EXCITED!!!! > > > dave stohler > www.picasaweb.google.com/das24rules > > > > _______________________________________________ > AMC-list mailing list > AMC-list@xxxxxxxxxxxx > http://list.amc-list.com/listinfo.cgi/amc-list-amc-list.com > _______________________________________________ > AMC-list mailing list > AMC-list@xxxxxxxxxxxx > http://list.amc-list.com/listinfo.cgi/amc-list-amc-list.com > _______________________________________________ AMC-list mailing list AMC-list@xxxxxxxxxxxx http://list.amc-list.com/listinfo.cgi/amc-list-amc-list.com